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1.
Environmental Health Engineering and Management Journal. 2015; 2 (1): 23-30
in English | IMEMR | ID: emr-174679

ABSTRACT

Background: Investigating the performance of naturally operated treatment plants may be due to the fact that they cannot be operated as desired, or that they should be modified to achieve good performance e.g. for nutrients removal. The advantage of kinetic coefficient determination is that the model can be adjusted to fit data and then used for analyzing alternatives to improve the process. This study investigates the efficiency of subsurface artificial wetland and determines its kinetic coefficients for nutrient removal


Methods: The present study investigated the kinetics of biological reactions that occurred in subsurface wetland to remove wastewater nutrient. Samples were taken from 3 locations of wetlands for 6 months. The nutrient content was determined through measuring Total Kjehldahl Nitrogen [TKN], ammonium, nitrate, and phosphate values


Results: Average levels for TKN, ammonium, nitrate, and phosphate in effluent of control wetland were 41.15, 23.59, 1.735, and 6.43 mg/L, and in wetland with reeds were 28.91, 19.99, 1.49 and 5.63 mg/L, respectively. First-order, second-order, and Stover-Kincannon models were applied and analyzed using statistical parameters obtained from the models [U[max], K[B]]


Conclusion: The nutrients removal at Yazd wastewater treatment plant was remarkable, and the presence of reeds in wetland beds was not very efficient in improving system performance. Other more efficient plants are suggested to be evaluated in the system. Stover-Kincannon kinetic model provided predictions having the closest relationship with actual data obtained from the field

2.
Environmental Health Engineering and Management Journal. 2014; 1 (1): 7-12
in English | IMEMR | ID: emr-174668

ABSTRACT

Background: Yazd waste stabilization pond facilities consist of three stabilization pond systems, module 1, module 2 and module 3 that AWSP module 1 has started its operation. The existing facilities have had several problems in their operation. The objectives of this research were to evaluate the performance of stabilization ponds in wastewater treatment of the city of Yazd, due to several problems in their operation, and to prepare a scheme of its upgrading, if necessary


Methods: During the period from December to June 2010, data analysis were carried out for both raw and treated wastewater


Results: Results of these investigations showed that the average effluent concentrations of Biochemical Oxygen Demand 5 [BOD[5]], Chemical Oxygen Demand [COD] and Suspended Solid [SS] taken from anaerobic pond and secondary facultative ponds of module 1 were 306.9, 135.18, 139.75 and 136.75, 69.025, 136.5 mg/L, respectively


Conclusion: These results indicated that the effluent of the anaerobic pond of module 1 was complied with the Iranian treated wastewater standards for agricultural reuse in terms of BOD[5] and COD concentrations; hence the secondary facultative ponds could be changed to other primary facultative ponds in order to increase the capacity of wastewater treatment plant

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