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1.
Braz. j. microbiol ; 45(2): 447-456, Apr.-June 2014. ilus, tab
Article in English | LILACS | ID: lil-723116

ABSTRACT

The interest in production of natural colorants by microbial fermentation has been currently increased. The effects of D-glucose concentration (3.18-36.82 g/L), inoculum size (12.5 x 10(9)-49.5 x 10(9) cfu cells/mL) and air-flow rate (1.95-12.05 L/L min) on the biomass, total carotenoid and canthaxanthin (CTX) accumulation of Dietzia natronolimnaea HS-1 in a batch bioreactor was scrutinized using a response surface methodology-central composite rotatable design (RSM-CCRD). Second-order polynomial models with high R² values ranging from 0.978 to 0.990 were developed for the studied responses using multiple linear regression analysis. The models showed the maximum cumulative amounts of biomass (7.85 g/L), total carotenoid (5.48 mg/L) and CTX (4.99 mg/L) could be achieved at 23.38 g/L of D-glucose, 31.2 x 10(9) cfu cells/mL of inoculation intensity and air-flow rate of 7.85 L/L min. The predicted values for optimum conditions were in good agreement with experimental data.


Subject(s)
Actinobacteria/growth & development , Actinobacteria/metabolism , Canthaxanthin/biosynthesis , Aerobiosis , Air , Bacterial Load , Batch Cell Culture Techniques , Biomass , Bioreactors/microbiology , Glucose/metabolism , Models, Statistical
2.
Eng. sanit. ambient ; 17(2): 143-154, abr.-jun. 2012. ilus, graf, tab
Article in Portuguese | LILACS | ID: lil-665939

ABSTRACT

Neste trabalho, avaliou-se o desempenho de um biorreator à membrana em batelada sequencial para a remoção de nutrientes (nitrogênio e fósforo) de esgoto sanitário. O reator, construído em escala piloto, foi operado durante 241 dias com tempo total de ciclo de 4 horas, sendo 5 minutos para alimentação, 55 minutos para a fase anóxica e 180 minutos para as fases de aeração e filtração (simultaneamente). Ao longo do monitoramento, foram empregados dois fluxos de filtração: 5,55 e 11,1 L.m-2.h-1, que resultaram nas taxas de troca volumétrica de 5 e 10%, respectivamente. As eficiências médias de remoção de Demanda Química de Oxigênio total, nitrogênio amoniacal e nitrogênio total alcançadas foram de 99, 98 e 96%, respectivamente. Em relação à remoção de fósforo, observou-se inicialmente um baixo rendimento do reator, sendo verificado ao longo do tempo, no entanto, uma tendência de melhora na remoção desse nutriente, atingindo eficiência média de 74% entre os dias 158 e 241. A utilização do fluxo de filtração de 5,55 L.m-2.h-1 proporcionou uma operação estável ao biorreator à membrana em batelada sequencial no que se refere à pressão transmembrana, tendo sido atingido o valor limite de 0,7 bar apenas uma vez em 181 dias de operação, ao passo que, com fluxo de 11,1 L.m-2.h-1, esse limite foi atingido 3 vezes em 55 dias.


This study evaluated the performance of a membrane bioreactor sequencing batch, in pilot scale, to remove nutrients (nitrogen and phosphorus) from domestic wastewater. The reactor was operated for 241 days with a total cycle time of 4 hours, with 5 minutes for feeding, 55 minutes for the anoxic phase and 180 minutes for the aeration and filtration phases (simultaneously). Throughout the monitoring, two filtration flows were employed: 5.5 and 11.1 (critical flux) L.m-2.h-1, which resulted in the volume exchange rates of 5 and 10%, respectively. The removal efficiencies of total Chemical Oxygen Demand, ammonia nitrogen and total nitrogen were achieved by 99, 98 and 96%, respectively. Regarding phosphorus removal, a poor performance was observed in the beginning of the experiment; however, a tendency of improvement in the removal of this nutrient was further verified, reaching an efficiency average of 74% between the operational days 158 and 241. The flux filtration at 5.55 L.m-2.h-1 has provided a membrane bioreactor sequencing batch stable operation in relation to transmembrane pressure since it reached the limit value of 0.7 bar only once in 181 operational days, while for 11.1 L.m-2.h-1 it was observed 3 times in 55 days.

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